My motor is suppose to be standard(the guy i bought it from just got it redone by nissan).
yeah i removed my choke on my old ford sapphire aswell not for performance but because i broke it hehe (my early days).
So i disassembled my carb(32/36) lastnight and made an interesting descovery. main jets:130/135 idle: 45/45 and i think 175/175 aircorrection. Thats a bit small for a 2L motor isn't it

but just right for a A14 motor
The carb was in horrible condition had white flakie stuff everwhere, jets where bloked and dirty as hel..l....now squeky clean. the only thing i couldn't get out was the emultion tubes only the back part came of with emultion tubes firmly stuck in carby

.
How is a person suppose to remove them if this happens?